Attendance:
Alex, Zach, Danielle, Charles
Goals:
All
- Drive robot and fix occurring problems
- Work on strategy
Meeting Notes
- Problems found:
- Strafing did not work
- Claw would not pick up blocks
- Linear lift would not go up because lift’s rack was loose
- Solutions:
- Tightened the meccanum wheels
- That did not fix the problem, but we figured out it might be a problem with the weight distribution
- Reshaped the metal claw support therefore reshaping the claw
- Tightened the rack on the linear lift
- Tightened the meccanum wheels
- Strategy:
- Figured out that we should get 3-4 blocks and when 20 seconds are left in the match we should attempt to get on the balancing pad for 20 points